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There are already a few pages that show you how you can fit the popular
Taig 4-jaw chuck to the Asian 7x10 (or 7x12) lathe. I too had a go. If
I made a mess of it, I could always buy another...
Here in the UK, you can buy a 4-jaw chuck from Machine Mart - the people
who sell the minilathe.
To my mind, the trickiest part was going to be cutting the recess to
fit the spindle plate without having to keep swapping them over. I decided
to make a simple template by making a disk exactly the same diameter as
the spindle. To avoid the same swapping problem, I mounted the disk on
a blank MT3 arbor. Now I could make the disk so that it was a good snug
fit into the existing 3-jaw. My spindle plate was 55mm diameter (2.165")
so, as soon as I got within a couple of thou, I took it nice and steady
until the desired fit was achieved. The only material I had to hand for
this was 3mm paxolin sheet. Less than ideal and probably not a good choice
but it did the job.
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A nice new MT3 blank in the spindle.
When I removed the existing chuck, one of the studs unscrewed from
the chuck not the nut. Irritating. The nut proved so tight, I had
to make a split nut to clamp the free piece of stud in vice grips
to get it undone. |
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First job is to turn down the stub so that
it will fit through the hole in the centre of both chucks. That way,
the new chuck can be fitted over the stub to check the fit and easily
be remounted to it if further work is required, As it happened, the
template disk was all that was needed. The arbor was drilled and tapped
to take the spindle template blank which was just screwed on with
a countersunk machine screw. |
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Very shortly, I had a spindle template
done. Paxolin cuts fairly easily and leaves a good finish. On the
back surface, you can see a feathery mess left behind. This is easily
removed |
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When finished, the template is remounted
to another mandrel for ease of handling. It fits in the 3-jaw with
a bit of a wiggle and measures up the same as the actual spindle to
less than 1/1000". |
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Right, now I was ready to attack the Taig chuck. A little patience
soon had the chuck mounted backwards onto the arbor and running
true to within a 0.0005 TIR.
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This was definitely the scary part. After all, this was the first
dimensionally critical piece of turning I had ever done and I was
a little unsure. The back of the chuck was fairly quickly recessed
to 4mm deep and 50mm diameter. Whatever it is made of, it cuts nicely.
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With most of the metal removed, I went as carefully as I could
with much pausing and figuring of handwheel movements until the
template just fitted.
In spite of my best endeavours, the recess was too big by about
0.001. Not bad I guess but not what I had hoped for. There was definite
movement in the template even though it would not drop out of its
own accord. |
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Scary part done, I moved on to what should have been the easy part
- fitting the studs. I really ought to have known better...
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Digging around in the scrap box revealed a suitable bit of steel
rod. This was soon converted into four pins sized to fit into the
spindle holes with a small conical pip at one end. With the pins
in the plate, the chuck was fitted over the spindle A bit of scrap
behind the pins and a sharp tap with a brass hammer (actually a
lump of bar stock) soon had locating spots on the chuck.
There was no need to harden the pins. They are one-shot disposable
items. |
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While cutting the pins to length, I wanted a quick way to reliably
move the saddle back and forth by known amounts.
I discovered that my six-inch rule just sits on the bed behind
the V-way without fouling the saddle. It is no trouble to read off
movement quite accurately and, of course, you have an easily resettable
zero.
The simplest things are so pleasing |
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Now things started to go a bit pear-shaped. I had a drill stand
for my hand drill and used that to make the first stud hole. I was
careful, mindful of the lack of rigidity, centre drilled and went
up in small steps. However, I was too stupid to check that the damned
thing was drilling perpendicular to the table. My beatifully inserted
stud was clearly at an angle other than 90 degrees and I could not
see how to get the rest of the holes in.
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After a bit of a break, I decided to mount the new chuck on a bit
of 5/8the steel bar clamped in the toolpost. I was not certain that
it would be sturdy enough but it worked like a dream. My drilling
was all done from the chuck with bits just held in the 3-jaw.
Here you see the centre drill hunting for its next victim. |
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A bit of brass scrap with a convenient hole made a fine support
for the back end of the tap to hold it square and I soon had a suitable
hole.
In the UK, the studs are M6. Everything except the leadscrew and
power supply is metric on mine. No problem here and, although it
is not convenient in many (largely historical) ways, there is a
certain simplicity to the metric system. |
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Once the stud were in, that was it - job done. The wobbly stud
was a bit of an embarassment. In the end I had to use three of the
holes from the 90 degree set and one from the 120 degree set. Bit
of a bodge, but balance is not much of an issue since the 4-jaw
is used specifically to hold stuff eccentrically.
Possibly as a result of the screw up, when the new chuck is mounted,
I can detect no movement against the backplate by hand. Once tightened
down, TIR is 0.0015. I guess I will live happily with that since
it is hardly critical for a 4-jaw anyway so long as it cannot move
against the spindle in use. I am fairly sure it can't - a tap with
the hammer will soon find out.
Overall, I am pretty pleased with the job. The way I have done
it may not be the best but it is pretty simple and taught me a lot
on the way. What more could you ask?
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